I just realized that I have not posted since October 23rd. There have been several updates. Also included were the Toronto Blue Jays' post-season games. That was a great reason to not post.
The areas that were touched
The nose wiring harness
The completion of the fog light connections and installation
The left engine mount
The Nose Harness
When I was fixing the front indicators, I noticed some other taped areas on the main harness. The left headlight pod decided it didn't want to drop. The high beam on the right side didn't work consistently. I tested the resistance between the headlights; there should be no resistance, since the lines are being fed from the same source before the fuses.
Some of the connectors that are in the engine bay for the pod, indicators, and headlights showed corrosion, are dirty, and some are damaged. It is very tight where these harnesses are located in the engine bay for working on. So, when doing any work, the harness needed to be freed. Also, I noticed that the harness grommets were toast. On the list to replace.
The right pod on the bench. This was actually pretty easy to pull out of the car. The upside was that the brackets left a mark on the bulkhead, which meant that getting the proper alignment was pretty easy when reinstalling
The connectors from the pod, you can see the corrosion on the pins. This is not great, since it creates a resistive point
With the pod out, I fished the harness out.
Some items to notice: the brown/blue wire, which is part of the control of the pod. Has no connector. The ground connector is 'dirty'. The connectors have overspray and are dirty. Below is the section of the wiring diagram for reference. It is easy to see the 'main' beam circuits and the connection before the fuses.
With the harness hanging out of the headlight opening
With the harness spread apart, the issues are easier to see.
One of the connectors 😞
When I was at the U-Pull, I grabbed some connectors and could replace some of the more damaged ones. Like this one
Just needed to pull the pins and put it in the sonic cleaner.
After some cleanup, such as 'polishing' the pins when they were pulled out of the connector, and some heat shrink tubing for additional strength, where some chaffing occurred. They were put back together.
In preparation for pulling the harness from the nose, the right-hand harness was pulled through the bulkhead. It didn't look great either.
On the right side decided to remove the harness tape. To check the state of the wiring.
For the most part, this looked fine. But the ends still need to be fixed. After cleaning up and re-taping, I thought it was ready for service again
Moving over the left side harness, it was 'bulging', so I pulled the electrical tape off, and this is what I found
This is not good. Need to pull the harness since these repairs are so close to the edge of the nose. And this
Taking off the tape, and well, it looks like a mess.
Here is the leap of faith: I am going to put as much of the harness in the sonic cleaner. I needed to move the cleaner to the front of the car. Here is the cleaner ready to go.
After a couple of minutes, it was showing what was coming off.
After about 30 minutes and heat the harness came out much cleaner
Having the wires being much cleaner, it is much easier to assess the damage that needs to be repaired.
Time to go through the wires one by one and do the actual repair. I have found the best, most reliable connection is to tin the ends of the wires, then use heat-shrink solder connectors. This provides the electrical connection, but it doesn't provide mechanical strength. For that, dual-wall heat-shrink tubing is used. The clue will seal the connection from moisture, and the tubing itself replaces the original insulation. An example of the chaffed wire
After cutting and tinning, the heat-shrink connector is added. It may not look perfect, but that is okay
The dual-wall heat shrink makes sure the connection is good.
In the end, the wires got fixed. Checking the resistance, in most cases, it is now 0.00ohms. A couple of them are 0.01ohms
My workbench while doing this
Once all the wires were repaired, they needed to be rewrapped. Foglights
One of the tasks was to clean up the OE foglight wiring and add foglights. The switch was pulled apart and cleaned. The wiring, red/yellow, was still in place. The original connector was a BL bullet connector. Not good enough, it got replaced with a Deutsch connector.
Plug it inWE HAVE LIGHT!!! This is the factory harness and switch. Now, there is a concern about running these lights and the amperage draw. These are LED, so they will be a lot less than the original lights. Looks like I need to find a rear fog light as well
Wiring Routing
With that test done and other tests, it is time to put the harness back in place. The best surprise was that the harness is pretty easy to route to the left side. The nose in front of the radiator can be reached to fish the harness across
Then the harness is fished through new grommets ( absolutely essential ). Ready to be plugged back together. The feed comes through one grommet, and the accessories come through another to meet in the engine bay
Lights!
Besides mounting the foglights, I wanted a set of auxiliary driving lights. I wanted a set of lights that other drivers can see. It seems all LBCs are too small, and in Canada, all new cars have DRL, Daytime Running Lights. And people do not see cars coming towards them without lights.
That is nice, but FIRE IT UP!
DAMN!!!!!!Moving to the next items